Riveted Spars and Ribs in Right Elevator

Unfortunately Jared was unable to make it over to work with me today. I’ll be docking his pay. 🙂

Work on the the left elevator is still halted until I have a means to rivet the hinge portion of the aft spar. To wit I have ordered a complete range of squeezer flush sets from Aircraft Spruce. They should be here tomorrow.

Significant progress to report on the right elevator however…

Riveted the rear spar and rib assembly to the bottom right skin.

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Actually some progress was made on the left elevator. I was able to rivet the ribs to the bottom skin as well as the trim doubler assembly.

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I riveted the skin to the rear right spar using the special bucking bar to reach the shop heads.

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Side view of the special bucking bar in action.

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I fabricated the tool called out in the plans but didn’t actually need it on the right elevator. Maybe it’s necessary on the left?

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I blind-riveted the top and bottom halves of the ribs together. I was able to reach the aft rivets with no problem.

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Here they are all riveted.

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I riveted the forward spar to the ribs.

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…And then riveted the skins to the spar with the squeezer.

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I riveted the skins to the and root ribs as well.

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Next I’ll glue the aft ribs in place with Pro Seal, install the trailing edge, shoot the last few rivets in the root and tip ribs and she’ll be done!

I had one oops today and a gripe with the plans. They remind you that the counterweight skins go under the elevator skins after you’ve already riveted the aft spar and the ribs. This made it impossible to correct. I tried to carefully pull the skin out and bend the counterweight skin up as little as possible but it left a bit of a permanent bend. Nothing tragic. Just annoying. It would have been more helpful if the plans provided this warning when they had me cleco in the forward spar assembly.

Today’s Time (hours): 4.5
Empennage Time (hours): 112.5
Total Time (hours): 112.5

 

Riveted Aft Spars to Skins

Began riveting the bottom top left skin to the aft spar.

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Everything was going great until I got to the part with the trim tab hinge. My bucking bar won’t reach around the hinge eyelets.

Side note: after all of this, I realized that the shear clip was supposed to be on the outside of the closeout tabs in the picture below. So ended up drilling it out and re-attaching it properly. Funny thing is that last week I mentioned to Jared and Wes that I thought it would look better on the inside. Subconscious got the better of me i guess.

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I thought of using the squeezer on these rivets but I only have two flush sets. One is too long and the other is two short. I hit up Jared and he’s got a flush set that’s halfway between the two. He volunteered to swing by tomorrow morning and do some building with me. So I set the left elevator aside until tomorrow.

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I moved on to the right side and riveted the bottom skin to the aft spar. I taped all of the rivets in place to back rivet the ribs. I shot one row but it’s really load and it’s getting late so decided to call it quits for the night.

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Today’s Time (hours): 2.0
Empennage Time (hours): 108.0
Total Time (hours): 108.0

 

More Work on Elevators

Jared Solomon and Wes Greer stopped by today and helped move the elevators along. I really appreciate having experienced builders helping me out.  Things went really fast and their advice is incredibly valuable. Had lot’s of fun building together, too. Thanks guys!

Today we final drilled the tip ribs to one another and to the counterweight skins. We cut the foam trailing edge and trim tab ribs. We trimmed and deburred the trim tab skins. We trimmed the right elevator aft spar. We bent the closeout tabs on the left elevator skin. We fit and drilled the trim tab hinge. We clecoed everything together and fit/trimmed the elevator trailing edges.

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Jared and Wes went home and I continued building. Not even ten minutes unsupervised and I screwed up! I misunderstood the interface between the trailing edge extrusion and the elevator wing tip. I removed way too much material from the trailing edge. I didn’t realize that the wing tip would be trimmed and butt up against the trailing edge. Had I read forward to the “Empennage Fairings” section, I would have understood how this went together. Oh well… Ordered a new trailing edge from Van’s.

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Today’s Time (hours): 5.0
Empennage Time (hours): 85.0
Total Time (hours): 85.0

 

Riveted everything together

I finished back riveting the stiffeners to the skins. I had one oops where a rivet got cockeyed just before I drove it. It left a ding in the skin but didn’t penetrate. I debated replacing the skin but opted to move on.

I used 3M F9460PC double stick VHB tape to secure the trailing edge extrusion to the skin and clecoed it together. I put some long rivets through every tenth hole or so, put the tape on both sides of the wedge, and used the rivets to properly register the taped wedge to the right skin. Then I clecoed it in place and removed the rivets.

I riveted the stiffeners and shear clips together. I removed the backing from the other side of the tape while I pried the skins slightly apart so the strip didn’t tear. I removed clecos as I worked my way to the top of the trailing edge. I pressed the left skin into the tape and clecoed every hole.

I mounted the counterbalance. I had to file a bit off of the forward corners to clear the shop heads of the rivets holding the counterbalance rib in place. I riveted the skin to the spar, and riveted everything else except the trailing edge. That will be tomorrow’s adventure.

I neglected to shoot progress photos along the way but here’s the result of today’s work…

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This is the tape I used…

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Today’s Time (hours): 6.0
Empennage Time (hours): 36.0
Total Time (hours): 36.0

 

Primed rudder parts, assembled spar, drilled trailing edge

I primed all the rudder parts and skins today. I picked up a roll of hardware mesh at Home Depot and put it up on some blocks over my paint table. I did this to keep all the small pieces from being blown around by the spray gun. It worked really well.

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All dressed up and no place to go!

 

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I got the shipment of VS replacement parts from Van’s today. Unfortunately only four of the five parts I ordered arrived. They shipped the wrong part for the fifth on. I ordered a VS-705 they shipped an E-705. I called and they’re shipping the correct one. Oh well. I’ll just continue on with the rudder until it arrives.

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I riveted together the spar, reinforcement plates, counterweight rib, bottom rib, rudder horn and shim. The I screwed up and riveted the rudder attach nut plates to the wrong side of the spar. Drilled them out and re-riveted correctly. Cost me six rivets and an extra thirty minutes. No harm no foul.

I’m still struggling with my riveting technique with the gun. There was one rivet on the rudder horn that couldn’t be reached with the squeezer. I managed to put a big smile into the rudder horn. I think it will be okay.

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I made a drill guide from a paint stirrer so that I could more accurately drill perpendicular to the chord of the rudder. I cut a 6 degree angle on the end and held it flush to the rudder and aligned the drill to the edge of the stick.

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Off to Vegas tomorrow for a conference. won’t be making ay progress until next weekend.

Today’s Time (hours): 6.5
Empennage Time (hours): 27.0
Total Time (hours): 27.0

 

One step forward, two steps back

Started off the day dimpling the vertical stabilizer skin with the DRDT-2. I’m pleased with this tool. Dimpling large parts like the skins is a piece of cake and the dimples are consistent. I will say that I am considering getting a c-frame as well. It would have come in handy for riveting the rear spar. Juggling the spar and the pneumatic squeezer was challenging. While the squeezer was workable, I think the c-frame would have been easier.

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Once the skins were complete, the fun began! I was dimpling the substructure when I decided that the VS-707 rib needed an extra hole. So I made one. With the pneumatic squeezer and dimple dies. I hammered out the unwanted dimple and made a doubler to fix the flange. I completed the rest of the dimpling uneventfully.

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I riveted the aft spar assembly together. This went well and I’m happy with the result.

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I riveted the front spar doubler to the front spar and clecoed the ribs to the front spar in preparation for riveting. And that’s when things went south again. I tried to rivet the root rib and the nose rib to the spar from the front of the spar to the back. Turns out that this is extremely difficult due to the angle of the nose rib. Even with an offset rivet set in the gun, I couldn’t get straight on the rivet. I tried to buck it anyway. The rivet folded over. The angle of the nose rib made drilling out the rivet problematic as well. I thought about drilling the shop head but it was too messed up to drill. I ended up mangling the hole beyond repair. Turned all three parts into scrap. I ordered replacements from Van’s and since I was already going through the process and paying for shipping I included a replacement VS-707 as well.

Lesson Learned: If it doesn’t seem right, stop and think about it. When I couldn’t get the rivet set square to the rivet, I should have stopped and considered shooting the rivet from the other side.

Today’s Time (hours): 6.5
Empennage Time (hours): 15.5
Total Time (hours): 15.5

Deburred and scuffed all the vertical stabilizer parts.

I’ve been using a single flute de-burring bit in my drill on the low speed setting to deburr all the holes. It seems to work pretty well. I hit it with about two turns and light pressure. That leaves a nice clean finish without enlarging the hole or leaving a visible chamfer.

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Today I dispelled the notion that this airplane is going to be perfect. I was trying to de-burr the edges of the skin on the scotch bright wheel and accidentally touched the other side of the skin to the grinding wheel. It hit the top corner of the skin and bent it a bit and took a nick out of the edge. I was able to straighten it. It was only bent a few degrees. I was also able to file the nick out of the edge. Probably not the worst mistake I’ll make. It only cost me about ten minutes.

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I picked up a bit extension from home depot yesterday so that I could use the de-burring bit on the insides of the flanges. This kept the bit sufficiently straight and produced an acceptable result.

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Used a maroon scotch bright pad and scuffed everything up. Ready for priming.

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Today’s Time (hours): 3.0
Empennage Time (hours): 7.5
Total Time (hours): 7.5